| 08
January 2003 - Air Midwest 5481 |
Air Midwest Flight 5481, operating as US Airways Express Flight 5481,
was a flight from Charlotte/Douglas International Airport in Charlotte,
North Carolina, United States to Greenville-Spartanburg International
Airport near the cities of Greenville, South Carolina and Spartanburg,
South Carolina. On January 8, 2003 a Beechcraft 1900D (N233YV) operated
by Air Midwest as US Airways Express under a franchise agreement used
for the route stalled after take-off, crashed into a US Airways hangar
and burst into flames 37 seconds after leaving Charlotte/Douglas International
Airport.
All nineteen passengers and two pilots aboard died in the accident,
and one person on the ground received minor injuries. None of the US
Airways employees working in the hangar received injuries
The NTSB determined the crash to have been the result of two separate
issues.
After take-off, the plane climbed steeply before stalling, despite
both pilots pushing the control column forward. The aircraft's most
recent service involved adjusting the elevator control cable, and was
performed two nights before the crash at a repair facility located at
Tri-State Airport in Huntington, West Virginia. During the investigation,
it emerged that the mechanic who worked on the elevator cables had never
worked on this type of aircraft. Investigation revealed that turnbuckles
controlling tension on the cables to the elevators had been set incorrectly,
resulting in insufficient elevator travel, leading to the pilots not
having sufficient pitch control. Although a post-adjustment control
test would normally be conducted to ensure proper operation, the maintenance
supervisor who was instructing the mechanic decided to skip this step.
The NTSB noted that the FAA were aware of the "serious deficiencies"
in the training procedures at the facility, but had done nothing to
correct them.
Although the pilots had totaled up the take-off weight of the aircraft
before the flight and determined it to be within limits, the plane was
actually overloaded and out of balance, due to the use of incorrect
(but FAA approved) passenger weight estimates. When checked, the NTSB
found that the estimates were over 20 pounds (9 kg) lighter than the
actual weight of an average passenger. After checking the actual weight
of baggage retrieved from the crash site, and passengers (based on information
from next-of-kin and the medical examiner), it was found that the aircraft
was actually 600 pounds (272 kg) above its maximum allowable take-off
weight, with its center of gravity 5% rear of allowable limits.
It was determined that neither problem alone would have caused the
loss of control, which explains why it departed Huntington, West Virginia
safely.
As a result of the weight issues discovered, the FAA planned to investigate
and potentially revise estimated weight values, something that had not
been done since 1936. Air Midwest now use an average weight of 200 pounds
(90.7 kg) per passenger, but the NTSB suggests that airlines use actual
weights instead of average. 70% of small air carriers still use average.
Air Midwest publicly apologized for the incident after the family of
crash victim Christiana Grace Shepherd pressured the airline to do so.

Download
the Cockpit Voice Recorder transcript